TY - JOUR
T1 - Optimization of a full-scale Unitank wastewater treatment plant for biological phosphorus removal
AU - Zhou, Zhen
AU - Xing, Can
AU - Wu, Zhichao
AU - Tong, Fei
AU - Wang, Junru
PY - 2014/3/19
Y1 - 2014/3/19
N2 - The Unitank process combines the advantages of traditional continuous-flow activated sludge processes and sequencing batch reactors, and has been extensively employed in many wastewater treatment plants (WWTPs) in China. Biological phosphorus removal (BPR) of a full-scale Unitank WWTP was optimized by increasing anaerobic time from 80 to 120 min in an operation cycle of 360 min and reducing solid retention time (SRT) from 21.3 to 13.1 d. The BPR efficiency of the full-scale Unitank system increased from 63.8% (SRT of 21.3 d) to 83.2% for a SRT of 13.1 d. When the anaerobic time increased from 80 to 120 min, the net anaerobic phosphorus release amount increased from 0.25 to 1.06 mg L -1, and sludge phosphorus content rose from 13.8 to 15.0 mgP·(gSS)-1. During half an operation cycle, the average specific phosphorus release rate increased from 0.097 mgP·(gVSS·h) -1 in 0-40 min to 0.825 mgP·(gVSS·h)-1 in 40-60 min. Reducing SRT and increasing anaerobic time account for 84.6% and 15.4% in the total increment of phosphorus removal of 1.15 mg L-1.
AB - The Unitank process combines the advantages of traditional continuous-flow activated sludge processes and sequencing batch reactors, and has been extensively employed in many wastewater treatment plants (WWTPs) in China. Biological phosphorus removal (BPR) of a full-scale Unitank WWTP was optimized by increasing anaerobic time from 80 to 120 min in an operation cycle of 360 min and reducing solid retention time (SRT) from 21.3 to 13.1 d. The BPR efficiency of the full-scale Unitank system increased from 63.8% (SRT of 21.3 d) to 83.2% for a SRT of 13.1 d. When the anaerobic time increased from 80 to 120 min, the net anaerobic phosphorus release amount increased from 0.25 to 1.06 mg L -1, and sludge phosphorus content rose from 13.8 to 15.0 mgP·(gSS)-1. During half an operation cycle, the average specific phosphorus release rate increased from 0.097 mgP·(gVSS·h) -1 in 0-40 min to 0.825 mgP·(gVSS·h)-1 in 40-60 min. Reducing SRT and increasing anaerobic time account for 84.6% and 15.4% in the total increment of phosphorus removal of 1.15 mg L-1.
KW - Unitank process
KW - biological phosphorus removal
KW - optimization
KW - solid retention time
KW - wastewater treatment
UR - https://www.scopus.com/pages/publications/84891828311
U2 - 10.1080/09593330.2013.850519
DO - 10.1080/09593330.2013.850519
M3 - 文章
C2 - 24645458
AN - SCOPUS:84891828311
SN - 0959-3330
VL - 35
SP - 766
EP - 772
JO - Environmental Technology (United Kingdom)
JF - Environmental Technology (United Kingdom)
IS - 6
ER -